Foreword: We and the boat are back home
in Fort Myers and we’re still being diligent about social distancing and
hygiene practices. Hopefully that’s true
for all y’all, too. But here in the USA, with most states
proceeding with “re-opening” without much regard for science, we’re also
preparing for a long slog with multiple setbacks looking very likely. If you want a historical analog, go study the
Spanish Flu outbreak of 1918…along with how & why it continued into
1920. Mark Twain reportedly once said
“History doesn’t repeat itself, but it often rhymes.” It seems we’re destined to prove him right
again. But there is good news….have
discovered if you keep a glass of scotch in each hand then you can’t touch your
face. That’s good hygiene.
This entry is all about a system repair
and nothing else. So unless you are a
boat geek, or bored enough to seek almost any distraction, you’ll want to skip
it.
Even though we’d had a very successful
maintenance stop with Yacht Tech in Palm Beach, we still had ample boat
projects to keep us busy on Ghost Rider. But the priority problem-to-solve was the
stabilizer oil overheating condition we had encountered at the midpoint of our
journey back to Fort Myers. After a few
days at the dock we now had a much cooler engine room, allowing for a
relatively relaxed and comfortable approach to troubleshooting…and the luxury
of temporarily disabling the main engine without consequence.
The design of the cooling circuit for
our stabilizer oil tank is relatively simple. Ghost Rider is an exception compared to most Nordhavns….rather than
being keel-cooled with a dry exhaust stack, our Nordy’s main engine is cooled
via a raw (sea) water heat exchanger and uses a traditional wet exhaust. That arrangement provides for a secondary
cooling circuit that branches off at the bottom of the main engine’s heat
exchanger and is then routed over to the stabilizer oil tank reservoir for
additional cooling duties there. After
exiting the stab oil tank, that auxiliary cooling circuit empties into the sea
via its own dedicated discharge thru-hull.
Except now we could not detect any outflow coming from that thru-hull
opening….meaning no cooling flow.
So there is a minor flaw in that
design: while the heat exchanger itself is
quite beefy, by necessity it utilizes two sacrificial pencil zincs (anodes) to
prevent galvanic corrosion inherent with that salty seawater flow…and as those
zincs decay (as intended) the shedding debris will descend to the bottom of the
heat exchanger – right where that stabilizer cooling loop begins. That loop uses much smaller diameter hosing
and piping (5/8” ID), and occasionally is prone to clogging with that decaying
zinc detritus. When that occurs the
result is hot stabilizer oil….rather than the normal 155F temps we were seeing
nearly 200F on the leg to Marathon following the overtemp warning light.
Rick decided to start the investigation
where the stabilizer cooling loop originates at the bottom of the main engine’s
heat exchanger. After removing the two
zinc plugs (they were due for replacement anyway) and disconnecting a segment
of the hose feeding the start of the stab cooling circuit, he stuck a high
pressure hose into the zinc ports for a flushing out. While that netted some debris it certainly
was not enough to cause a blockage or overheat issue.
After reassembling the main engine side
of the loop, the next step was to check at the opposite end of the stabilizer
cooling circuit, where it exited the boat via the thru-hull fitting. It was a likely suspect since there was a 90
degree elbow where the outflow hose clamped to the thru-hull fitting – and in
there Rick found enough stray zinc debris to form a very effective dam. A stiff wire coat hanger server as a suitable
plumbing auger, and in the end that blockage turned out to be the only
culprit. After clearing the clog and
starting the main engine we observed good cooling flow exiting from the
thru-hull discharge.
The Yellow Arrow Points Out the Resulting Normal Stab Cooling Flow from the Thru-hull. |
The question now was whether such an
event could be prevented in the future.
The zinc decay itself is a critically important feature that protects
expensive diesel engine parts from dissolving through galvanic corrosion; it
would not be wise to change that portion. One option was to design an entirely
separate cooling loop for the stabilizer oil tank, which would entail a new intake thru-hull as well as a new
electric water pump (and then sealing off the existing feed from the heat
exchanger.) But another path was just to
insert a sea-strainer device into the existing cooling circuit to trap zinc
debris, with periodic inspection and cleaning.
The latter sounded a whole lot easier and cheaper, at least as a first
try. So that’s the approach we’ve taken
for now. Rick installed a standard
Jabsco PumpGuard strainer at the circuit’s low point, close to where it
branches off the main engine’s heat exchanger.
It was a relatively simple modification,
but it needs to be sea-trialed to determine whether it still allows for an adequate
flow rate for cooling the stabilizer oil tank. A better long-term solution might also call
for an inline shut-off valve just upstream of the strainer to allow cleaning of
the strainer basket without having to first shut down the engine and drain the
heat exchanger (that beast holds a LOT of sea water.)