Foreword: We’re still observing our healthful
Covid protocols and staying safe, although here in Florida a lot of folks seem
intent on making that increasingly difficult.
Hurricane Isaias isn’t helping any, although thankfully we are not
directly impacted by that.
The Aeroshell Aerobatic Team Flies Their AT-6 Texans with Beautiful Precision |
Apart from trying to keep the
boat clean, keeping up with routine maintenance, and occasionally exercising
engines and systems, our focus this month has been trying to find a fix for the
busted crane up on the boat deck. But first
we’re going to back up and start at the beginning of the month.
Independence Day!
As
a three generation military family every July 4th we appreciate and
enjoy our Independence Day celebration.
It’s a fabulous USA holiday that celebrates the beginning of a marvelous
experiment, albeit one in some jeopardy these days. We flew Old Glory both at the condo and the
boat all day, and respectfully retired the colors at sunset. In between we made sure we were at the marina
to witness the celebratory flyover by the Aeroshell Aerobatic Team (LINK), in their precision
fourship formation of AT-6 Texans directly over Ghost Rider. That vintage WWII aircraft (in service since 1938) is
the one in which Rick’s father learned to fly back in the early ‘40’s before
deploying to the Pacific Theater….and deserves its own salute. Short amateurish video below.
Regular
Maintenance
A
few days later it was time for our periodic “running of the diesels”, normally
not a routine with which we need to be concerned, but which is worth mentioning
during a time when so many boats and boaters (like us) are stuck in port. While Nordhavn vessels and their Lugger
diesels have proven to be largely indestructible, our goal is to minimize the
expensive service opportunities along the way.
Keeping systems exercised helps with that.
Just
running an engine for a few minutes does more harm than good – failing to bring
it all the way to the normal operating temperature range will just promote
internal condensation, corrosion and the early demise of both coolant and
oil. In reality that requires running
them for at least 30 to 45 minutes, and where possible under load.
The Genset Instrument Cluster, with the Yellow Arrow Highlighting the Much Too High Temperature Gauge Reading of 210F |
That means activating as many engine-driven
systems as possible and exercising them as well. For the main engine that includes the
stabilizers and alternators, as well as bumping into gear for working the
transmission and packing gland. (You
want to be double-tied to very sturdy dock cleats for this part.) For the wing engine that entails running the
hydraulic thrusters. And for the
generator we disconnect from shore power and run full electrical loads. Finally, the steering system – helm pumps,
steering ram and autopilot pump – all get a short workout, too.
Break/Fix
Opportunities
During
the generator exercise period we noticed its coolant temperature gauge was
reading high – up to 210F, well above its optimum target of 185F (its thermostat
opens at 180F). Shooting the engine’s coolant
expansion tank with the infrared temperature gun confirmed that it was indeed
running at normal temp, so we knew we had some sort of gauge issue and not an
actual mechanical problem. (The genset
also has an internal fail safe switch that automatically shuts down the unit at
205F.) It was time for some sleuthing.
The Back End of the Generator Where the Ground Wires Terminate. Yellow Arrow Indicates Gauge Grounding Bolt, Green is for the Bonding Wires. |
We
had learned from the Nordy owners forum that this wasn’t a particularly unusual
problem, and that just replacing the gauge rarely if ever resolved the
problem. While the sending unit was a
possibility, that wasn’t likely either – when that goes wonky, it’s usually a
total failure. It was much more probable
that one or more ground wires on the engine needed attention, and in the end
that proved true in this case. On our
L843 (12 KW) generator Rick eventually located two 10MM bolts securing a total
of three grounding wires plus three other bonding wire straps at the junction
box bracket. Disassembling those and
then thoroughly cleaning, sanding/filing, and then coating the ring terminals
with dielectric grease before reassembling did the trick. Rick also rearranged them a bit to isolate
the smaller grounding wires from the larger bonding straps.
The Genset Instrument Cluster, with the Yellow Arrow Now Highlighting the Improved Temperature Gauge Reading of 190F Following Ground Wire Removal, Cleanup & Reattachment. |
The
genset’s temp gauge still reads slightly high compared to the IR gun reading,
but knowing that analog gauges aren’t particularly accurate in the first place,
we can live with it. (This is the reason
that in most cars you now mostly see either “idiot lights” instead of gauges,
or at best their gauges have rather wide pointer ranges in between “low” and
“high” pegs at the extremes. The gauges
with precise graduations are rarely better than false advertising, better to
treat them as trending indicators.)
Now,
about that busted crane. At the end of
last month’s blog post we mentioned that our Aritex HSC-610 davit had developed
an onerous problem – we traced a nasty hydraulic fluid leak to a corroded
reservoir tank in the base of the unit. Rick subsequently determined that it was
likely electrically related (electrolytic) corrosion….the green bonding strap
attached to the metal tank was carrying voltage and current according to the
multimeter, and that’s a problem. Rick pumped remaining hydraulic fluid out of
the tank, then spent a few afternoons reviewing manuals (which were mostly
useless) and trying to discern how to dismantle and extract the tank, motor,
manifold and control box; but without much success.
The Crane's Hydraulic Motor and Tank Reservoir After Removal From Inside the Base. It Was Tight Quarters. |
We
learned from the marina office that Ross at nearby Classic Marine (who had very
capably handled our electronic throttle replacement last year) was experienced
with hydraulic cranes and davits, so we invited him out to the boat for a
look. He dug right in and had the motor
& tank assembly removed and on its way to his shop after about two hours of
sweaty persistence.
We’re
not exactly sure what the ultimate resolution may be, or when. For now Ross has agreed to work it in to his
busy schedule, but thus far hasn’t had any luck locating compatible replacement
parts. So we’re trying to look at
the bright side: at least it didn’t expire while we were trying to launch or
retrieve the dinghy. We still have no
idea what we would do about a crane failure with a 450 pound rigid inflatable
suspended from it, especially at some remote anchorage.
Project
Work
The next “future project” to bubble to
the top of the list was to upgrade the boat’s five Racor fuel filter
assemblies. Ghost Rider was originally built at a time that preceded today’s
ABYC and US Coast Guard standards for fire protection, which now specify filter
housings must either be all metallic, or the clear plastic ones should be
protected by metallic heat deflectors. The objective is to make them survivable
for a minimum of 2 ½ minutes in the event of an engine room fire, giving the
fire suppression system time to do its thing before a breached (melted) filter
could dump a full fuel tank into the blaze.
There’s a good explanatory article HERE
from Passagemaker.com.
Rick’s goal was to retrofit the Racor “MA”
series of heat deflectors to our old “FG” series of filters. On the surface that appeared straightforward
and less pricey than buying five new primary fuel filters. And, as usual, the reality turned out to be a
bit different. Research revealed that
the Racor fuel bowl design was changed in the 2002-2003 timeframe (when Ghost Rider was built), and the older
model bowls are not compatible with the MA heat deflector kits; there could be
differences both in thread sizes as well as the o-ring gland required to properly seal
the bowl’s new brass plug. But the only way to tell was to drain the bowl and
remove the old plastic plug.
Rick used one of the smaller 500FG
filters (for the wing engine) as an initial test, ordering the heat deflector
kit and a new bowl out of an
abundance of caution. As it turned out
the new bowl wasn’t needed, but Rick swapped it out anyway. He also had to remove the fuel lines, move an Algae-X filtering device, and add spacers between the filter housing the
engine room bulkhead to create enough room for the deflector shield…so it was a
bit more involved than originally anticipated.
Typical boat project.
Removing & Replacing the Fuel Bowl on These Older Models is No Fun...the Upper Turbine Assembly Has to be Disassembled to Get That Done. |
Finally, Rick also added a brass on/off fuel valve (draincock), replacing the standard bowl plug, to make future draining both easier and less messy. To maintain conformance with ABYC fire standards that valve not only had to be metallic, but also could turn no more and no less than 90 degrees, could not rely on any spring tension for leak integrity, and also had to have its own plug as an additional measure against leaks.
We used the Racor Store (LINK) for the deflector kits and
bowl, and McMaster-Carr (LINK)
for sourcing the UL Listed fuel valves.
After running the wing engine for a spell and thorough leak-testing over
a few days we declared victory for the initial test. Rick proceeded to convert the bigger 900FG
Racor for the fuel transfer (polishing) system as a second test and that, too,
ended well.
In our August blog post we’ll report on
the efforts to convert the remaining three Racor filters (the two 900’s for the
main engine, and the other 500 for the generator.) And hopefully by then we’ll have a better
idea on next steps for the boat crane.
Next Month We'll Get the Conversion Done for the Main Engine's Dual Racors (Far Left) and for the Generator (Far Right). The Latter Won't be Fun Because of the Algae-X Filter Below & Behind It. |
Afterword: We can't tell which disease is more dangerous, Covid-19 or Utter Stupidity. Either way, we have plenty of both down here. Back in March we accurately predicted the
havoc that results from a leadership vacuum, but it seems we underestimated the
additive impact of sociopathic idiocy. Historians
won’t be kind, and neither will our future generations.
Hurricane Isaias Stayed Off to Our East. Only Four More Months Remain in the "Season". |